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One Year After MIEEIP's Audit

 

Benefits

"Buying boilers used to be like buying a pair of shoes, whether you buy size 5 or 8, the price is still the same. So, we just went for the largest size, after all, the price is cheap."
- Tritex managing director Richard Y. K. Chin


For more than 20 years, the management of Tritex Containers Sdn Bhd thought that it was okay to have big boilers for its production process, simply because big and cheap meant they were getting value for money. Little did they realise that oversized boilers were causing inefficient use of energy, which eventually meant the company was losing money.

Tritex, which manufactures corrugated paper to produce packaging boxes, opened its doors to the MIEEIP team in October 2001 to conduct energy audits, because the pulp & paper sector is one of the most intensive consumers of energy. Initial findings by the audit team showed that the company had the potential for energy savings as high as RM174,000 a year. The MIEEIP's engagement of Tritex is the first systematic attempt at improving energy efficiency.

Savings from energy efficient measures

The MIEEIP team discovered that most of the energy losses occurred because of uninsulated pipes in the boiler and leakages in the compressed air system and main distribution loops. The factory's waste treatment plant (WTP) was also located quite far from the boiler at about 140m, which resulted in heat loss at the piping.

The measures that were recommended, involving no-cost and low-cost investment included:

Fine-tuning boiler operations

Repairing leaks in distribution pipes and consumption points

Rectifying leakages in compressed air system

Shutting-off compressor and dryer during non-production hours

Using smaller compressor during low production period

Switching off all nonessential idling equipment

Improvement measures involving the efficiency of the boilers are replicable throughout the industry and can be implemented at minimum cost. For instance, the factory has decided to relocate the WTP closer to the boiler.

With an initial investment of only RM44,500, Tritex put in place a more efficient system that resulted in an annual energy savings of RM89,464. Table 1 shows the estimated annual savings from the measures implemented to date.

Table 1: Estimated annual savings for no-cost and low-cost energy efficiency measures

(Source: MIEEIP Energy Audit Team Follow-Up, 2002)
*Waste Treatment Plant

According to Chin, the factory expects to implement the measures, including the more complex ones within the next three to five years. The high cost measures may be in place in the next two years considering the overall financial slowdown, especially in the manufacturing sector. The company, said Chin, is basically saving now for other projects later, or to offset any rise in costs in future, such as for raw material.

(Source: MIEEIP Energy Audit Team Follow-Up, 2002)
*Waste Treatment Plant