In 2000, Daishowa America implemented
an improvement project on the effluent pumping system
at its paper mill in Port Angeles, Washington. Because
of chronic maintenance issues and rising energy costs,
personnel at the Port Angeles mill decided to review
the pumping system for optimization opportunities.
The review led mill personnel to implement a system-level
project that decreased the pumping system's energy
consumption. The project involved the installation
of mechanical Adjustable Speed Drives (ASDs) on two
pumps in the mill's pumping system. The project allowed
the system to operate more effectively, and resulted
in annual energy savings of $32,000 (RM 121,600) and
700,000 kilowatt-hours (kWh). The project also eliminated
many problems that led to excessive maintenance costs
and resulted in annual maintenance savings of $10,000
(RM 38,000). Because the project received partial
funding from the Northwest Energy Efficiency Alliance
(NEEA), the total mill project cost was $60,000. With
a total annual savings of $42,000 (RM 159,600) , the
simple payback was slightly more than 15 months.
COMPANY/PLANT
BACKGROUND
Daishowa America is the U.S. subsidiary
of Daishowa Paper Manufacturing Company, Ltd., of
Japan. The Port Angeles Mill in Port Angeles, Washington,
is an integrated pulp and paper mill. The mill uses
wood and recycled pulp to produce approximately 160,000
tons of directory papers annually. The company primarily
sells the paper to publishers of telephone directories
throughout the United States.
The effluent pumping system at the
Port Angeles mill is vital to the mill's production
process because it treats the wastewater created by
the paper manufacturing process. The system has three
100-hp (horsepower) centrifugal pumps. Prior to the
project, two of the pumps operated in parallel to
pump all of the raw effluent from the main pump station
sump to a clarifier. The third pump was used as a
backup or during extreme process upsets. The mill's
treatment process requires a minimum flow rate of
4,800 gallons per minute (gpm) (0.30 m3/s) to be reliable.
PROJECT
OVERVIEW
At the suggestion of NEEA, staff
at the Port Angeles mill agreed to a review of the
effluent pumping system to determine whether the system's
control scheme could be improved. Although the minimum
flow rate required by the treatment process was 4,800
gpm (0.30 m3/s) , the review showed that when both
pumps operated at full load, their combined capacity
was 7,000 gpm (0.44 m3/s). The excess 2,200 gpm (0.14
m3/s) was being recirculated back to the sump.
The size of the pumps and the system's
control scheme caused the excess pumping. The primary
system control was a level control in which a throttling
valve and a bypass valve worked in tandem to maintain
a minimum level in the sump. As the level in the sump
rose, the throttling valve opened and the bypass valve
closed. Conversely, as the level in the sump fell,
the discharge valve closed and the bypass valve opened.
Controlling the pumps this way required
starting them at full load from a dead start. This
created flow surges and pipe hammer that led to stress
in the system's piping. In addition, starting the
pumps from a dead start caused a long duration of
locked rotor currents, which overheated the pump motors.
The reviewers found that cavitation
and excessive vibration were present in the piping
because the pumps operated at full capacity. Although
the pumps were moving 2,200 gpm (0.14 m3/s) in excess
of the process requirements, the total volume moved
was still too small given the pump operating speed.
This disparity led to further process-piping fatigue
and shortened equipment life. Reviewers also discovered
that one of the parallel pumps drew significantly
more power than the other. As a result, plant personnel
took the pumps apart to inspect the impellers and
discovered that the impellers were severely worn,
which caused the pumps to operate less efficiently.
PROJECT
IMPLEMENTATION
Mill personnel decided to implement a system-level
project based on the review. The project centered
on installing mechanical ASDs, replacing the worn
impellers on both pumps, and upgrading the pump instrumentation.
The ASDs would replace the throttle and bypass valve
operation and would match the system's output to the
mill's requirements
Several factors made the selected
mechanical ASDs more suitable for the mill's environment
and needs than electronic Variable Speed Drives (VSD).
One factor that made this ASD model attractive was
its easy installation. The ASD installation simply
required moving the pumps back on their bases. and
installing spacers between the motors and the pumps.
No inverter-duty motors, extensive rewiring, or reconfiguration
of the pump stations were necessary. Second, ruggedness
and a lack of sensitive electronic parts made these
mechanical ASDs less prone to maintenance problems
in an environment such as the mill's effluent treatment
process. Because the mill's system is a medium-voltage
application, these ASDs were less costly than comparable
VSDs. Finally, these ASDs are mechanical, so there
are no direct connections between the motors and pumps;
this substantially reduces vibration and allows softstart
capability.
PROJECT
RESULTS
The implementation of the project
has improved the operation of the effluent pumping
system and resulted in significant energy savings
for the Port Angeles mill. With the newly configured
pumping system, the mill no longer depends on bypass
and throttling valves to control the pumping system.The
ASDs can vary the pump speed to match the pump output
capacity with the mill's required process flow rate.
The new configuration allows the mill to base load
only one of the pumps while operating the other one
at partial load. By not operating both pumps at full
capacity, cavitation and vibration have been drastically
reduced. Because they are uncoupled from the pump
motors, the ASDs allow the pumps to start gradually,
which eliminates water surges and pipe hammer. This,
in turn, lessens stress on the system's piping and
internal components, reduces maintenance needs, and
prolongs equipment life.
The system's flow rate has declined
by 31 percent, or 2,200 gpm (0.14 m3/s) from 7,000
gpm (0.44 m3/s) , and rarely exceeds 4,800 gpm. Power
demand has declined from 142 kW to 62 kW. The reduction
in the system's flow rate and power demand are due
to the installation of the ASDs, the rebuilt pumps,
and the operation of one pump at partial load versus
two pumps at full load. The mill saves $32,000 (RM
121,600) and 700,000 kWh in annual energy costs, and
$10,000 (RM 38,000) per year in maintenance costs.
Because of a cost sharing arrangement in which NEEA
funded a portion of the mill's project cost, the mill's
total cost for the project was $60,000. The simple
payback was slightly more than 15 months.
LESSON
LEARNED
The proper control scheme is critical
for the efficient operation of a pumping system. Relying
on bypass and throttling valves to control a pumping
system can lead to energy waste and excessive maintenance
requirements. At the Port Angeles mill, the use of
bypass and throttling valves led the mill to operate
its pumps at a greater capacity than necessary, and
in ways that created unnecessary stress on the process
piping and internal system components. Operating the
pumps in this manner caused the system to waste energy
because it moved 2,200 gpm (0.14 m3/s) in excess of
the process requirements. The improvement project
on the Port Angeles Mill's effluent pumping system
reduced the system's flow rate by 31 percent and allowed
one pump to operate at variable load. These changes
reduced energy consumption. In addition, the project
eliminated sources of stress on the system's process
piping and on the pumps' internal components, resulting
in lower maintenance costs and increased equipment
life.
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The
Mechanical ASD
The
ASD installed by Daishowa America is a non-electronic,
mechanical device that is usually placed between
a motor and the load the motor is driving, whether
it is a pump, fan, or blower. The drive consists
of two independent components that have no physical
contact with each other. One component, a rotor
assembly containing permanent magnets, is mounted
on the load shaft. The second component, a copper
conductor assembly, is connected to the motor
shaft. Relative motion between the magnets and
the copper creates a magnetic field that transmits
torque through the air gap between the components.
The width of the air gap can be changed, which
allows the amount of torque transmitted between
the motor and load to be continuously adjusted.
This allows precise speed control, including
soft starts and stops. Because of the lack of
adirect mechanical connection between the motor
and load, the ASD also eliminates wear-and-tear
caused by vibration. This ASD is well-suited
for medium-voltage applications in harsh environments,
and for drives in which efficiency is linear
with speed, such as fluid drives.
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