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Holistic approach to EE at Pan Century Edible Oils

 

Benefits

bullet 35,000 GJ in annual energy saving from steam system optimisation
bullet Reduced steam consumption by 10 percent
bullet Reduced power demand at four cooling towers by 8 percent
bullet Average payback period of 1 year to 2 years
bullet Monitoring and targeting for continuous improvements
bullet Total energy cost saving of RM1 million from four EE projects

Summary

Pan-Century Edible Oils (PCEO) Sdn Bhd, a manufacturer of oil refinery products and specialty products, is one of the 48 factories audited by the MIEEIP team under the Energy Audit Programme. The factory’s monthly energy bill amounts to RM2 million. The aim of the audit is two folded, namely, to identify energy cost saving potentials and transfer the auditing skill to the staff of PCEO. Jointly, the MIEEIP audit and the PCEO energy management teams identified several potential energy cost saving measures. A combination of measures recommended by the MIEEIP and PCEO’s energy teams on steam management, cooling tower modification, energy-use monitoring and targeting, and the replacement of standard motors to high efficiency motors are discussed here as local case studies for industrial energy efficiency.

Project Overview


PCEO commenced its operations in Malaysia 25 years ago, and to date has 13 plants at a single location in Pasir Gudang, Johor. Its total manufacturing capacity of oil refinery products and specialty products is about one million tonnes. The factory recorded an annual turnover of RM 750 million in 2002. This internationally recognised company, which is a member of the Aditya Birla Group, has a workforce of 285 people.

The company had already established a Focused Improvement Project Team (FIPT) prior to the collaboration with MIEEIP. FIPT, which was tasked with overall improvement strategies, responded positively to several MIEEIP recommendations on steam management and implemented them systematically. Its initiatives on other energy efficiency improvement areas are ongoing and closely monitored for comparisons against established norms under the in-house Purta or benchmarking system.

Project Overview

Project One : Steam optimisation


More than 550 tonnes of steam is generated daily for physical refining, making soap noodles, tank farm heating and fractionation. During the audit, the team identified significant steam leakages and analysed the respective losses. To minimise these losses and to implement other energy cost saving measures, the management embarked on a RM 1.0 million venture. To date, the steam optimisation programme has alone resulted in an annual energy cost saving of RM680,481. Other measures that were already initiated by PCEO are modifications to the factory’s cooling towers; replacement of standard motors with high efficiency motors; steam conservation schemes, heat recovery schemes and monitoring & targeting, which produced a total energy cost savings of RM320,000. PTM has agreed to do the study of compressed air system and chilled water system.


Background

PCEO operates four units of boilers to supply steam to the refining and soap noodle plants. Steam is generated at a cost of RM50 per metric tonne, whereby 90 percent of the cost component is for fuel purchase while maintenance, chemical treatment and water consumption make up the balance 10 percent. About 55kl (kilo litre) per day of Medium Fuel Oil (MFO) is consumed. Realising the immense benefits of the energy saving measures and in view of the increasing fuel and water costs, PCEO embarked on a holistic approach to optimise the existing steam supply and demand structure. Steam saving target was set at 10 percent and to facilitate this, the FIPT immediately got to work to further confirm and implement the energy saving measures.

Project Implementation

The energy saving measures identified by the team for the steam supply and demand system were divided into no, low, and high cost categories. PCEO used both its in-house financial resources and expertise to implement the identified Energy Cost Reduction Measures (ECRMs) in stages since May 2002. The high commitment and seriousness showed by the factory’s top management ensured the full completion of the projects within an eight-month period. Through monitoring and verification, the savings were quantified and reviewed on a monthly basis for the following measures:

I. Use of low pressure steam (3.5 barg) for tank farm heating and tracing lines in place of medium pressure steam (14.5 barg)
Audit findings
The maximum temperature required for tank farm heating and tracing lines is between 70° and 80° C , which can be attained with low-pressure steam. Currently the heating is carried out using medium pressure steam.
Measure recommended To convert the current heating system heating to low pressure
Action Taken The present medium pressure header was provided with pressure regulating valves to supply low pressure steam for tank farm heating
   
ll. Installation of pressure regulating valves for steam to distillation vacuum plant
Audit findings:
The design vacuum pressure for the distillation plant is 10 barg at a steam header pressure of 13.5 barg. This combination of settings resulted in higher steam consumption amounting to 24 percent.
Measure recommended:
To supply the steam at an optimum pressure of 10 barg.
Action taken:
Pressure regulating valves were installed in the acuum circuits to maintain the steam supply pressure at 10 barg.
   
III.Insulation improvement
Audit findings
An insulation survey for the entire plant was carried out to identify areas of insulation losses. It was found that many steam lines were not properly insulated.
Measure recommended:
To carry out an audit of the steam distribution system to determine the various sizes of insulation to inimise the losses and rectify the steam leakages.
Action taken:
All condensate return lines, valves, and fittings were provided with correctly sized insulation to prevent heat losses. The temperature difference between the pipe surface and the ambient, maintained at around 10°C after the rectification, not only saves energy but also creates a thermal-comfort working environment.
   
IV. Steam trap maintenance
Audit findings: Steam traps were found either under sized or leaking due to the lack of maintenance. This in turn contributes to the ineffectiveness of the entire steam distribution system.
Measure recommended: Conduct a survey on the existing steam traps and replace the under sized ones, and establish a steam trap periodic maintenance system.
Action taken: Suitable sized traps were provided and a strict steam trap checking procedure was implemented to detect faulty traps before installation
   
V.Condensate recovery
Audit findings:
The steam condensates at the various points of use were not recovered, because of possibility of oil contamination. This again contributes to the low efficiency of the combined boiler and steam distribution system.
Measure recommended:
Pipe all the condensates to suitably installed intermediate tanks before transferring them to the soft tank for reuse in the boilers
Action taken:
Intermediate tanks and a pump were installed to collect and transfer the condensate to the existing soft water tank for reuse in the boilers. This resulted not only in fuel savings but also savings in water treatment chemicals.
   
VI. Temperature control for heating tanks
Audit findings:
Although the required heating temperature of the tank farms is only 80°C, due to continuous charging of the steam the temperature raises up to 95°C. The rise between 80°C and 90°C not only contributes to energy wastage but also affects the quality of the contents of the tank farm.
Measure recommended:
A temperature controller system should be provided to ensure no excess steam is charged to the tank farm.
Action taken:
A temperature controller system to cut in and out the steam charging at 78°C and 80°C respectively was installed. This can be considered as good energy management practice.
   
VII. Replacement of steam ejectors with vacuum pump in PC1 bleacher unit
Audit findings:
It was noticed that steam ejectors were used to create the 70 Torr vacuum pressure in the bleacher. This indirect method of converting steam pressure to create vacuum is highly energy inefficient.
Measure recommended:
Outsource for suitable system that will create direct vacuum pressure.
Action Taken:
A water seal ring type vacuum pump, which is a proven energy efficient method for creating vacuum pressure, is installed.
   

Result

The energy and cost savings as well as the CO2 reduction achieved from the implementation of the above ECRMs is shown in the following table. On the whole, steam consumption at PCEO was reduced to 35 metric tonnes/day from the above schemes.

Energy Cost
reduction
Type
of
Invest-
ment
Fuel
Savings
GJ/yr
CO2
Reduction
t/yr
Capital
Expen-
diture
Annual
Cost
Savings
RM/yr
Payback time
(yr)
Use of low pressure steam for tank farm
heating
low cost 2665 197 60,900 71,152 0.9
Pressure reduction valve for distillation
vacuum system
low cost 6,504 481 28,000 122,551 0.2
insulation improvement low cost 10,789 798 47,000 203,275 0.2
Steam trap saving maintenance low cost
4,789 325 77,500 78,725 1.0
Condensate recovery low cost 2,943 218 118,000 73,964 1.6
Temperature control for tank farm heating low cost 1,896 140 23,600 34,648 0.7
Replacement of steam ejectors with vacuum
pump in bleacher
low cost 5,188 384 45,000 96,166 0.5
Total
  34,380 2,544 400,000 680,964 0.6


Project Two : Cooling Tower Modification


Background

Seven cooling towers are located strategically in the fractionation, physical refining and soap noodles plants. Cooling water is used mainly in crystallisers, heat exchangers for cooling process fluids, compressor intercoolers and after coolers and condensers. The performance of the cooling towers in the fractionation plant was investigated and it was found that energy savings of 25 percent could be achieved by implementing thermal efficiency improvement measures in this area.

Project Implementation

The following weaknesses were found at the cooling towers:

i  
The cooling towers were designed for 38°C return water temperature and 30°C cold-water temperature at 27°C wet bulb temperature.
However, as against design temperature drop of 8°C, the actual cooling was 5°C at 26°C wet bulb temperature. Therefore, the cooling load achieved was only 60 percent of the design capacity.
ii  
The liquid to gas (L/G) ratio was at 0.8 and 0.86 for cooling tower no.1 and 2.67 for cooling tower no.2. The recommended L/G ratio for tropical climatic condition is between 1.0 and 1.1. The L/G ratio can be improved by increasing the blade angle of the fans to increase the flow rate.
iii  
Due to lower differential temperature, 3 cells were in use to get the desired heat duty.


The poor performance of the cooling towers was due to the condition of the fills and bad distribution of water. The fills are also broken and displaced from their position due to sagging. The combined effect of these defects streams the water through the cooling tower instead of being broken into fine particles, which is a pre requirement for efficiency in heat removable from the returned hot water.

The improvements to the cooling towers are being carried out in phases. The existing seven wooden fills were replaced with PVC fills whereas the FRP fan blades have replaced aluminium fan blades as they are lighter and provide effective blade angle management. The blade angle of the fan was fixed at around 16°
C to maintain an optimum air velocity of 9m/s.

Project Three: High Efficiency Motors

Background

High Efficiency Motors (HEMs) are generally two to four percent more energy efficient than standard motors. The paybacks on HEMs are high when they are incorporated during the initial installation stages of the plant. However, replacing an existing standard motor just before its life cycle can justify the HEM option. Apart from this, HEMs can be considered as a preference instead of rewinding an existing standard motor. Usually the loss in efficiency resulting from rewinding amounts to two to three per cent.

Project Implementation

At PCEO, a programme to replace the existing standard motors to HEMs was started in 1994 in a phased manner. The replacement was done in stages and as of today, most of the standard motors in the plants have been replaced by HEMs. Though the purchase price of HEMs is about 20 percent more, PCEO achieved a significant decrease in the electricity consumption over the years. According to them, the top management was instrumental in the success of this programme, as they believed the additional price (or premium) could be repaid by the energy cost savings from the motors with higher efficiencies.

The economic feasibility of investing in a new HEM is calculated using a common method called “simple payback”.


Simple payback (yr) = price premium/electricity cost savings






An example of such calculations is shown in the table below for one of the existing standard motors that was replace recently

NO
Item
Unit
Figure
1 Base data    
1.1
1.2
1.3
1.4
1.5
1.6
Motor size
Efficiency of standard motor (at 75% full load)
Efficiency of HEM (at 75% full load)
HEM price premium
Operating hours
Average

kW
%
%
RM
hr/yr
RM/kwh

75
91.50%
93.90 %
2,450
8400
0.22

2 Post implementation results    
2.1
2.2
2.3
2.4
Reduced power demand
Annual power consumption saved
Electricity cost savings
Simple payback time
kW
kWh/yr
RM/yr
yr
1.57
13198 2904
0.84

Table 2: Sample calculation

The total investment cost for the replacement of all the existing standard motors to HEMs was RM400,000. This investment was quickly recovered within four years.



Project Four : Energy Monitoring & Targeting

Background

As a management driven activity, the company has implemented a Monitoring and Targeting (M&T) system to support the Birla Group’s World Class Manufacturing (WCM) philosophy – If you can’t measure, then you can’t manage. According to Pan-Century’s joint president Mr. S.C Jain, the M&T exercise directly detects abnormalities for immediate remedial actions. This in turn results in energy savings, which otherwise would not have been realised due to the delay in detection of the same manually. Norms are established for consumption trends and weekly targets are set and monitored closely.

Every month, the established figures are compared against the actual consumption or output at the management meetings. Follow up actions for abnormalities are addressed in the meetings. The findings and the analysis of the data gathered from the M&T system are reported to the headquarters for further scrutiny. If targets are not met, justification is sought and peer factories will be contacted for assistance. Otherwise, the company strives to improve its operations to meet the set targets.

Project Implementation


The M&T system is part of the parent company’s Purta system, which has been in practice for years in all aspects of manufacturing and performances. It is a benchmarking system established based on design point consumption values. These are ideal values computed for every set of production parameters such as material inflow, product output, utility consumed and waste generated. At PCEO, M&T is carried out plant wide and at sub-process levels. The company is in the midst of completing the installation of an online monitoring system for energy consumption. Phase One of the project has been completed with the installation of the metering equipment at every supply and consumption point.

The second phase, involving the centralisation of the electronic energy data feedback and reporting system through local network, is ongoing. The company has purchased several metering equipment such as the maximum demand controller, which was installed in April 2003; kWh meters; steam flow meters and the chiller load controller. Installation is being done in-house.


Project Implementation

The total cost of metering is approximately RM17,000 for the maximum demand controller (RM3,000); steam flow meter (RM12,000 per unit) and chiller load manager (RM 2,000). No expenses were incurred for the installation and commissioning or the development of the M&T software as they were done entirely by the staff.


Management-driven commitment towards EE


At a recent interview, Pan-Century vice president (Engineering) Mr. P. R. Goyal explained that energy efficiency is deployed through the company’s policy to attain total customer satisfaction at minimum cost. He said: “Energy, which cost the company RM2 million monthly, is one of the cost components that can bring maximum return on investment related to energy efficiency. We are also committed to a greener environment through the efficient use of natural resources,” Mr. Goyal added.

This high level commitment was affirmed by Mr. Jain. He explained that the management would approve EE projects even though some of them had long payback periods. He said the determining factor in approving such projects is the potential for plant improvements as well as the contributions towards social and environmental benefits. The company has approved self-financing for many low- and high-cost EE improvement projects in the past. Now the company is totally convinced that such projects are not only viable but also beneficial to the company. Mr. Jain emphasised, “There are no restrictions to the budget allocation. As long as we are convinced of the overall benefits to the company, an energy efficiency project will be approved immediately.”