In 1996, the H.B. Reese Company successfully
implemented an upgrade of its compressed air system
at its production facility in Hershey, Pennsylvania.
Once the project was completed, the plant was able
to take two compressors totalling 150 horsepower (hp)
offline while increasing output and product quality.
The project resulted in a 4 percent reduction in annual
energy costs and lowered maintenance costs due to
the increased operational efficiency of the newly
configured system. With the project's total cost of
$310,000 (RM1,178,000), and annual savings of $108,000
(RM410,400) per year, the plant achieved a simple
payback of less than 3 years. In addition, due to
better quality control, the plant was able to increase
production by 15 percent without having to bring additional
compressors online.
Benefits
| a.
Saves 1.87 million kilowatt-hours (kWh) annually |
| b.
Saves US$108,000 (RM410,400) in annual energy
costs |
| c.
Reduces energy use |
| d.
Increases production by 15 percent |
| e.
Improves product quality |
| f.
Reduces maintenance costs |
Application
Compressed air systems are found throughout
industry and consume large amounts of electricity.
Maintaining a stable and consistent flow of air is
critical to the performance of any industrial compressed
air system. The true pressure requirements of end-use
applications in a plant should determine the system
pressure level.
COMPANY/PLANT
BACKGROUND
H.B. Reese is a subsidiary of the Hershey Foods Corporation,
producing confectionery products, such as chocolate-covered
peanut butter candies. The Reese plant in Hershey,
Pennsylvania, is a 47,000 square-meter facility with
900 employees. The facility doubled in size between
1957 and 1970 to accommodate the increase in demand
for its candy products. Compressed air is important
for the production process, because it is needed to
operate the cylinders on the wrapping machines and
robotic applications. These end-use applications require
very clean, moisture-free compressed air at a consistent
pressure level in order to operate reliably. Prior
to the project, the Reese plant had to operate their
compressors at a discharge pressure of 7.5 bar gauged
(barg) so that the robots and cylinders would receive
air at the minimum acceptable pressure level.
PROJECT
OVERVIEW
In 1995, the Reese plant commissioned
a professional survey of its compressed air system
because it was not able to generate compressed air
at the consistent pressure level needed for reliable
production. The survey led to a comprehensive strategy
to improve the plant's compressed air system's efficiency
and performance.
The survey found a number of issues
that prevented the plant's compressed air system from
operating optimally. As the plant's manufacturing
capacity had increased over time, additional compressors
were added. By the time of the survey, the plant had
a total of thirteen 75-hp rotary-screw compressors
housed in various areas of two buildings. Because
the buildings were not connected to each other, the
plant effectively had two compressed air systems that
were operating independently of each other. The survey
showed that if the two systems were to be connected
into one system, it would generate and deliver compressed
air more effectively.
Next, the survey found that the plant's
compressed air system experienced considerable pressure
loss between the compressors and the end-use applications.
This caused the system's pressure level to fluctuate
widely and led to inconsistent pressure at the points
of use. Pressure loss/drop is a function of a compressed
air system's dynamics-the interaction of airflow rate
with the inherent resistance of the pipeline and air
system components. The main factors that led to the
Reese plant's pressure drop were leaks in both the
plant's distribution piping network and components
in the system such as filters, regulators, lubricators,
hoses, and fittings. In addition, some of the components
were improperly sized for the airflow and pressure
that they were supposed to provide.
The leakage load at the time of the
assessment was 20 percent of the compressed air system's
out-put. Another 15 percent of the system's output
was being consumed unnecessarily in open blowing applications.
In addition, solenoid-operated condensate drains allowed
air to escape, causing the system pressure to fall.
The combination of leaks, inefficient components,
leaking condensate drains, and open blowing applications
caused the pressure level to fluctuate by 0.8 to 1.5
barg between the compressors and the production equipment.
When temporary demand events occurred, the pressure
level declined further and additional compressors
were brought online to bring it back up.
The factors that caused the plant's
pressure drop were also causing over 5,700 liter per
minute of artificial demand. Artificial demand is
the excess air required by a system's unregulated
uses because the system is being operated at a pressure
level in excess of actual production requirements.
In this case, the artificial demand that was created
by the leaks, undersized components, and unregulated
point of use operations required the system pressure
level to be set at a much higher level to maintain
minimum acceptable pressure for end-use applications.
Finally, the survey found that the
system's dryers were overloaded when the compressors
operated at high or low temperatures. This caused
some moisture to carry over into the system. The survey
recommended installing coalescing filters to mitigate
this situation.
PROJECT
IMPLEMENTATION
To address the problems in its compressed
air system, the plant implemented a system level improvement
project that incorporated many of the survey's recommendations.
The first and main action item was
to connect the two systems and overhaul the piping
network that fed the production equipment. Following
the survey's recommendations, the plant centralized
the location of its compressors within each of the
two buildings and then connected both systems with
a 3 inch pipe. The plant also modified and replaced
undersized components such as filters, lubricators,
fittings and hoses, all located near the end uses,
for maximum rate of airflow. This lowered the minimum
pressure level needed by the production equipment
from 6 to 5 barg.
Next, the plant installed two pressure/flow
controllers, one for each building, along with 38,000
liters of storage capacity in two tanks. In order
to manage the compressors more effectively, the plant
upgraded its controls by installing a more sophisticated,
programmable logic control system and linking it to
the pressure/flow controllers.
As the plant began to lower the system
pressure, the leakage rate became less severe. Nevertheless,
the plant performed a leak detection and repair project
in which they fixed the most significant leaks in
the piping network. This allowed the plant to further
lower its system pressure. In order to address the
overloading of the dryers, two large coalescing filters
were installed just after each pressure/flow controller.
In addition, the plant retrofitted its open blowing
applications with vortex nozzle tips to reduce air
consumption.
RESULTS
The compressed air system improvement
project at Reese's plant in Hershey, Pennsylvania,
resulted in energy savings, better product quality,
and increased production. Prior to the project, the
plant operated 13 compressors at full capacity, with
aggregate horsepower totalling 975 hp. Once the project
was completed, the newly configured system operated
so efficiently that it only needed 11 compressors
totalling 825 hp. The energy savings were 1.87 million
kilowatt-hours (kWh), or over $87,000 (RM330,600)
per year. This represents 4 percent of the plant's
annual electricity costs. There were also savings
of over $21,000 (RM79,800) from reduced maintenance,
making the total savings $108,000 (RM410,400) and
leading to a simple payback of less than 3 years.
More importantly, because the product quality improved,
the plant produced less waste, which helped the plant
increase production by 15 percent without adding more
compressors to the system.
The facility was able to take some
compressors offline because of the new lower system
pressure. The plant was able to lower the system pressure
because the reconfigured piping and the re-engineered
distribution components lowered the system pressure
drop. The installation of the pressure/flow controllers
with storage stabilized the system pressure. The plant
is now able to operate the compressors at 6 barg instead
of 7.5 barg and delivers compressed air consistently
to the production equipment at 5 barg.
LESSONS
LEARNED
An improperly configured industrial
compressed air system prevents optimal system performance
and leads to increased waste by-product, energy waste,
and higher operating costs. In the case of the Reese
plant, the incremental addition of compressor capacity
over a number of years led to an arrangement of compressors,
piping, and undersized distribution components that
prevented the system from delivering its full potential
airflow at the desired pressure level. The operational
solution had been to add compressors in order to boost
the plant's ability to maintain the needed pressure.
Once the plant modified its system by linking the
two systems together and reengineering the distribution
components more optimally, the compressed air system
was able to perform more effectively, which led to
considerable energy savings and improved production.
PROPER
CONFIGURATION OF DISTRIBUTION SYSTEMS COMPONENTS
|
Often the importance of the components that make
up a compressed air system's distribution network
is underestimated. To deliver compressed air to
end use applications at the required volumes and
pressure levels, it is essential for the entire
distribution system to be properly configured.
Incomplete and improperly sized or configured
piping networks increase resistance to the airflow,
making the compressors work harder than necessary
to provide air to the end uses at required pressure
levels. In addition, distribution system equipment
that connects end-use equipment to the system
header equipment such as filters, regulators,
lubricators, hoses and fittings must be properly
engineered and sized for maximum rate of flow,
not flow per cycle. If the equipment is not engineered
this way, these components can become a compressed
air system's greatest source of pressure drop.
A properly configured and adjusted distribution
system will allow for optimal airflow through
a compressed air system. |
