Benefits
 |
Total energy savings of 57,300 Giga Joules/annum from the new
furnace and 2,800 Giga Joules/annum from improvements in two
annealing lehrs |
 |
Savings in fuel oil cost of more than 33 percent from heat recovery
system for the glass furnace
|
 |
Reduction in water consumption by 25 cubic metres per day through
recycling |
 |
Total investment of RM7.5 million and annual savings of RM 1.8
million |
Summary
Investing more than RM7 million, JG Containers (M) Sdn Bhd (JGC)
is one of the leading factories to have implemented energy
efficiency (EE) projects. This glass container manufacturer
undertook a series of low-cost and high-cost EE improvement
measures in an immediate response to the recommendations from
the energy audit carried out by the Malaysian Industrial Energy
Efficiency Improvement Project (MIEEIP) team at its facility.
Two years since the audits in August 2001, the factory has rebuilt
its furnace with a better control and heat recovery system, resulting
in a reduction of fuel consumption by 33 percent, or 57,300 Giga
Joules (GJ) per annum, and a significant improvement in the quality
of glass.
The modification of the operation of the annealing lehrs, a process
unique to the glass industry, brought about further annual savings
of RM120,000. One lehr, powered by electricity was modified
while another similar one was replaced with a natural gas powered
lehr.
Measures were also introduced to recycle water, which brought about further savings of RM17,500 per annum.
PLANT OVERVIEW
JG Containers (M) Sdn Bhd, a medium-sized glass container
manufacturing company with a workforce of 300 employees,
is one of the 48 factories audited by the MIEEIP. JGC
commenced its operations in Malaysia 31 years ago and its
manufacturing capacity of glass containers is about 120 tonnes
per day. The annual turnover for the year 2000 was RM 24
million with different forms of energy costs representing 20
percent of the total turnover.
PROJECT OVERVIEW
Furnace
The glass furnace at JGC experienced high losses because of
poor heat recovery from the exhaust and losses from the side
walls of the furnace.
The fuel consumption of a furnace depends on three factors:
1. Design and construction;
2. control of the furnace operation (percentage of cullets,
excess air etc.); and
3. ageing (adequacy of maintenance as it ages).
The main design criteria are the insulation of the outside walls,
and preheating temperature of the combustion air using heat
recovery from the exhaust gases. In addition, the loss of heat
to exhaust must be kept at a minimum by excess air control.
The old furnace at JGC lacked the control systems resulting in
higher losses. Besides, the surface heat losses were also high
due to the poor technology available back in 1992 to improve
the insulation of the surfaces.
The MIEEIP audit report was an eye opener to JGC as the audit
compared the Specific Energy Consumption (SEC) in JGC
against that for the US, UK, Thailand and Germany. These
figures were used as the benchmark to meet, while the JGC
management negotiated with suppliers for the furnace
rebuilding and renovation in the year 2002. At that time, the
SEC of melted glass at JGC was 7.08 GJ / tonne for the old
furnace. JGC then adopted the latest advanced crown system
for the furnace crown to reduce the heat losses.
Lehr
The annealing of glass, which is the slow cooling to minimise
the appearance of stress defects, is an important step in the
production of all glass. It is one of the more energy-intensive
processes, and the energy audits conducted at JGC revealed
high levels of losses whereby the SEC was as high as 0.13 GJ/
tonne of heat consumption at the annealing lehrs.
Recycling of water
The factory consumes about 100 cubic metres of water daily
as drinking water; service water for cooling purposes; and to
clean the cullets. About 25 cubic metres are used daily for
washing the cullets alone and discharged into the drain. The construction of a new filtration system enabled the factory to
recycle the water, thus saving 25 cubic metres daily.
Project Implementation and Results
The glass furnace was rebuilt with a better control and heat
recovery system from M/S Asahi Glass Japan in October 2002,
resulting in an increase in output from 90 tonnes per day (TPD)
to 120 TPD of melted glass. The total investment for the whole
project was RM7 million with a simple payback period of about
four years. For this process, the SEC reduced to 4.94 GJ /
tonne of melted glass from the initial 7.08 GJ / tonne.
Following the audit recommendations, JGC immediately
reconditioned one of the annealing lehrs at a cost of RM50,000,
which resulted in energy savings of 750 kWH per day. The
annual costs savings is approximately RM57,000, making the
project attractive with a simple payback period of less than
one year. The production too increased substantially by
reconditioning the annealing lehr. The SEC before and after the reconditioning project are 0.13 GJ / tonne and 0.075 GJ /
tonne of glass, which is equivalent to energy efficiency
improvement of about 42 percent.
One of the old annealing lehrs was replaced with a new energy
efficient LPG / NG-fired lehr at a cost of RM 400,000 in
November 2002. This resulted in net savings of RM62,000
per annum in energy cost, giving a simple payback period of
6.5 years. Production increased by about 50 percent. The SEC
reduced to 0.042 GJ / tonne from the previous figure of 0.13
GJ / tonne. The new lehr shows a more dramatic energy
efficiency improvement of about 67 percent.
These measures have also substantially reduced the CO2
emissions.
In order to recycle the water, a simple tank (size: 6m x 2m x
2m) was installed with a filter to remove the sediment and
grit before water is recycled for cullet washing. The cost of
the installation was RM18,000, and the savings achieved is
RM 17,000 per annum.
Energy Saving Measure
|
Investment
(RM) |
Energy
Savings (%) |
Simple
Payback
Period (yr) |
| Rebuilding furnace with
control systems |
7,000,000 |
33 |
4 |
| Modification of oneannealing lehr |
50,000 |
42 |
<1 |
| Natural gas-poweredlehr |
400,000 |
67 |
6.5 |
| Water recycling (cost saving measure) |
18,000 |
25 |
1 |
Table 1: Summary of energy saving measures
Specific energy consumption
The total fuel and energy consumption of JGC was analysed
for the year 2000, the first six months of 2001 and for the first
two months of 2003 according to “good glassware and melted
glass”. “Good glassware” refers to the net products or
packaged goods while melted glass refers to the gross glass
pull drawn from the furnace. With the energy saving measures,
the SEC for both the good glassware and melted glass reduced
from 13.4 GJ/t and 7.08 GJ/t at the start of the energy audit
exercise to 9.96 GJ/t and 4.94 GJ/t respectively.
| |
SEC (GJ/tonnes) |
Energy Saving Measure
|
Before |
After |
| Annealing Lehr (modification) |
0.13 |
0.075 |
| Annealing Lehr (Replaced with natural gas fired Lehr) |
0.13 |
0.042 |
| Glass furnace (Rebuilt with effective controls) |
7.08 |
4.94 |
Energy Conservation Projects Under Consideration
JGC is fully committed to energy conservation and is
considering other EE improvement projects for
implementation. The proposed projects mainly involve fuel
switching to optimise on the economic, technical and
environmental benefits of natural gas. This will include the LPG fired
equipment for the remaining electrical annealing lehr and
glass melting furnace. The use of natural gas will result in energy
cost savings, improve the processes, increase productivity and
improve emission norms.
In addition, JGC is keen on the segregation of compressed air
supply systems to meet actual requirements, and to replace one
low pressure compressor with a high efficiency compressor. The
plant requires low pressure and high pressure air for forming the
bottles. The factory’s air compressors are now operating at a
higher pressure, which is then throttled using pressure
regulatorsto reduce the air pressure.The saving expected from
the segregation of compressed air requirement and by installing
a low pressure air compressor is about RM50,000 per annum
with an investment of RM120,000.